by Jim
Schill
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The
Grundocrack pipe bursting tool is launched into the entry
pit. The small entry pit and flexible nature of the HDPE
replacement pipe were a perfect match for this job.
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Ask just about any good business
and they will tell you that time is money. General Motors is
a good business and they know all too well the value of time.
So when Al Brown, facility engineer at the Advanced Technology
Vehicles Division of GM in Torrance, California, realized that
something was drastically wrong with the company's sewer system,
the potential for disruption of the plant and loss of man hours
did not sit well.
The Advanced Technology Vehicles
Division in Torrance is a 172,000 square foot research and design
facility. It has the capability to produce engineering quantities
of actual product. The Torrance facility produced the first
electric car built from the ground
up. The plant's 180 employees work on everything from specs
and design to actual product testing. The loss of even one day
or a major disruption at the plant would be very costly.
Problems
with the plant's sewer system had been going on for quite some
time. GM purchased the building in September of 1991. Back then,
calls to the local sewer and drain service happened once a year.
Over the next few years the frequency increased from once a
year to once every six months, eventually to every three or
four weeks. Restroom facilities were backing up. Sometimes blockages
were caught early enough to prevent damage. Other times they
were not so lucky.
Brown knew
that something needed to be done. In November of 1996, a video
was shot of the plant's 4 inch VCP sewer. Using a small fiber
optic camera, a drainage contractor was able to look inside
the pipe. At that time, the pipe was getting to a point where
replacement was warranted. A year later when a second video
was taken, it was determined that the pipe would have to be
replaced. The video revealed tree roots, blockage and a deteriorating
pipe that would not last much longer. The video also showed
severe pipe displacement that Brown attributes to seismic activity
over the years. "After all," Brown says, "it's
California."
A coffee room was the scene of one
of the last encounters with the failing sewer pipe in the fall
of 1997. According to Brown, the coffee room was originally
a small restroom with a commode and a sink. It was later converted
into a coffee room. One afternoon, an employee noticed that
the coffee he had just poured into the sink was not going down
the drain. In fact, it was backing up. The employee also noticed
that there was a considerable amount of water around the base
of one of the cabinets in the room. The lateral sewer line was
completely blocked.
Replacing a pipe in that situation
is no small task, but there are options that can reduce the
enormity of such a project. The existing 4 inch VCP sewer needed
to be replaced with a 6 inch polyethylene pipe. The new pipe
had to be 330 feet long with 5 service lines. A 330 foot trench
through the plant was not feasible. A trenching application
would necessitate a completely different route for the pipe,
besides, the idea did not appeal very much to Brown. After some
consideration with their facility plumber, Doty Bros. Equipment
Company of Norwalk, California, was contacted.
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A
Doty Bros. crew member prepares each segment of the 330-foot
replacement pipe using a pipe fusing machine.
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After doing a cost and site analysis,
Doty Bros. project manager Bernie Monette and Al Brown decided
to use a trenchless applicationpipe bursting. The pipe bursting
process has become a popular method of pipe rehab. It effectively
displaces a fracturable host pipe, while simultaneously guiding
in a replacement pipe. In this particular case, a pipe bursting
job would keep disturbance around the plant to a minimum and
let the replacement pipe follow the same path as the old pipe.
It would also allow the job to be completed within the plant's
small window of opportunity (December 24 - January 5) and maybe
most importantly, cost about 50% less than a trenching job.
Torrance is a suburb of Los Angeles.
Located just a few miles from the Pacific Ocean, the soil is
loamy clay, very soft and silty and some of the area is just
plain sand. Monette was thankful that they did not run into
any seriously sandy conditions on this job. What they did run
into was extremely tight working conditions. The layout of the
plant resembles a letter "L" rotated clockwise 90 degrees
(see diagram). Throughout the 330 foot run, the Doty Brothers
crew needed to avoid Melaleucas trees, the parking lot, medians
and landscaping obstacles.
Monette planned to pull the pipe
into the short corner of the "L", around the trees, into
the launch pit and underground, 7 to 11 feet deep. The pipe
would then travel the length of the building, to the exit pit
where the pipe would be attached to the sewer main 25 feet underground.
An HDPE replacement pipe, teamed with a pneumatic pipe bursting
tool, was the perfect choice for working in such tight quarters.
Before the project could even begin,
it needed approval from Torrance's Building and Safety Department.
Senior plumbing inspector Jon McClannahan was familiar with
the pipe bursting method, however the 1994 Uniform Plumbing
Code did not have any specific language regarding the pipe bursting
process. After receiving written materials, including job specifications,
from Doty Bros. and GM, the plan was approved under section
301.2 of the Uniform Plumbing Code.
McClannahan explains, "That
section covers new and alternative methods and materials. While
there is nothing specifically related to pipe bursting in the
code, this provision allows for the use of new types of technology.
We certainly do not want to inhibit the advancement of technology
or the use of that technology by certified and qualified individuals."
After the city's approval, Monette
consulted the gas and electric utility associations to make
sure they would not encounter any surprises. With the help of
Brown, Monette and his crew identified the location of the sewer
pipe, as well as launch and exit pits. The project was now underway.
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Diagram
of the Torrance, California GM plant.
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After small launch and exit pits
were dug, the actual pipe burst was a breeze. The Doty Bros.
crew used a Grundocrack PCF 145 5.7 inch diameter pneumatic
pipe bursting tool from TT Technologies of Aurora, Illinois.
The Grundocrack was guided along the 330 foot burst by a 10-ton,
constant-tension Grundowinch, also from TT Technologies. This
type of winch supplies hydrostatic constant tension to ensure
that a constant speed is maintained no matter what the pipe
bursting tool encounters while traveling through the old host
pipe.
The actual burst at the GM plant
took a mere six hours. The new 6-inch SDR 17 HDPE pipe easily
made all corner bends and went in without a hitch. The new pipe
was connected to a chimney drop into the main sewer line 25
feet underground. The blocked lateral from the coffee room in
the plant was eventually cleared. According to Brown, when the
line was flushed, a host of interesting items vacated, including
years of coffee grounds and a 4-foot-long tree root.
The new pipe needed to pass a water
test after it was installed. According to McClannahan, the test
is designed to check the integrity of the new pipe and the integrity
of the lateral joints. The pipe is capped and then filled with
water. After it's filled, it must maintain a constant level
of water. This ensures that there are no leaks and that the
lateral joints are also leak free. The new pipe passed without
a problem.
The Doty Bros. crew had been working
with TT product specialist Collins Orton for some time and had
successfully completed four other pipe bursts with the Grundocrack
system before this one. Monette, who has been in the pipeline
rehab business for 20 years, says the technology is impressive
as well as cost efficient.
McClannahan was impressed by the
project as well and says pipe bursting and other trenchless
applications look to be the wave of the future, especially for
public entities that deal with water and sewer lines on a regular
basis.
After the pipe passed the tests,
the launch pits were refilled and the plant was operational
by the January 5 deadline. Al Brown received a letter of commendation
on the project from GM and was happy to be part of another pipe
bursting success story.
Cleaner,
May 1998
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