By Jim
Schill
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The
Grundocrack Goliath enters the launch pit for the
first run of 440 feet. Fourteen-inch HDPE pipe was
used as a bypass, paralleling the run.
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When the town of Hillsborough, California
needed to replace its aging sanitary sewer system, the project
received a tremendous amount of scrutiny. Sections of that system
run parallel to large Hetch Hetchy water transmission mains.
In addition, part of the system is located in an environmentally
sensitive area along the San Mateo Creek. So not only was the
project closely, so was the pipe replacement method the town
chose to replace the ailing system, pipe bursting.
The Hetch Hetchy watershed is the
main source of water for the city of San Francisco and surrounding
areas, supplying over 85% of the area's water. Water is transported
from the watershed, located in Yosemite National Park, through
large diameter water transmission mains, ranging in size from
49-inches to 79-inches. The San Francisco Water Department is
understandably protective of this vital system.
Hillsborough is located just south
of San Francisco. Recent flow studies showed that the gravity
fed sanitary sewer system was no longer able to meet the capacity
needs of Hillsborough's 11,000 residents. As a result, the town
hired Carollo Engineers, P.C. of Walnut Creek, California to
design capacity improvements for their system. Carollo Engineers
is an environmental engineering, consulting and design firm
experienced in cutting edge trenchless technology and infrastructure
design.
Carollo identified a 4,000-lf section
of the sanitary sewer system as a major problem area with significant
deterioration. That section runs through a right-of-way maintained
by the San Francisco Water Department. In addition to housing
the water departments Hetch Hetchy water transmission mains,
the area itself is a potential habitat for several endangered
species.
According to Project Engineer Jennifer
Glynn, the system was very undersized. Glynn said, "Hillsborough's
collection system consists of approximately 82 miles of
sanitary sewer pipes ranging in size from 6 to 18 inches.
Two L&L studies showed the 50 year old plus system to be
capacity deficient. Peak flow was estimated at 8.9 million
gallons per day. The existing system was sized to handle
approximately 5.5 million gallons."
An open cut replacement method would
require approval from a multitude of environmental agencies
as well as extensive documentation, both of which would add
time and cost to the project. Open cutting would also make the
potential for negative environmental impacts to the creek likely.
In addition to environmental concerns,
the diameters of the existing pipes needed to be increased as
much as three nominal sizes in order to raise the system's capacity
to desired levels. Pipe bursting offered an economically feasible
and environmentally sound solution.
Because of the large amount of upsizing
(15-inch VCP to 28-inch HDPE in most areas) and the extremely
deteriorated condition of the existing system, a pilot run of
660 feet (of the 4,000-lf section) was chosen to test the effectiveness
of pipe bursting.
Glynn said, "We also wanted
to start on a small scale because we were working so close
to the Hetch Hetchy water mains. We knew the San Francisco
Water Department was very concerned and would be monitoring
the burst closely." The project was awarded to D'arcy
& Harty Construction, Inc of San Francisco.
D'arcy and Harty is one of the most
experienced pipe bursting contractors in the San Francisco Bay
area. They have successfully completed thousands of feet of
pipe bursting in challenging situations including a much-publicized
burst at the famed Lawrence Lab on the Berkeley Campus.
According to Mike D'arcy, this
job presented several challenges. D'arcy said, "We
have completed large diameter bursts before, but never an
upsize of this magnitude. We also had to contend with tight
access, but ultimately we felt confident about the success
of the job." For additional technical support D'arcy
enlisted the help of Pipe Bursting Specialist Collins Orton
from TT Technologies, Aurora, Illinois.
For this job, D'arcy and Orton chose
to use an 18-inch diameter Grundocrack Goliath pneumatic pipe
bursting tool, a Grundomudd bentonite/lubrication mixing and
delivery system and 20-ton constant tension Grundowinch from
TT Technologies.
Orton said, "We needed a tool
that would have enough power to complete the upsize. Also, winch
selection was key. The Grundowinch provides constant tension
at variable speed. That means the winch is able to make adjustments
for conditions that affect line speed during operation, providing
constant, consistent and smooth pulling force which is essential
for successful pipe bursting."
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The
D'arcy & Harty crew used a McElroy butt fusion
machine to fuse the HDPE to the 18-inch diameter Grundocrack
Goliath with a 34.5 - inch expander.
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Before any bursting could begin,
the D'arcy & Harty crew searched for existing utilities. According
to Glynn, the crew was required to pothole entire sections of
the run where the sewer line and Hetch Hetchy water line were
closer than five feet apart.
Glynn said, "This was done
to eliminate the potential for lateral earth pressures or
detrimental vibratory earth movements generated by the pipe
bursting tool. Based on previous studies, we did not anticipate
any problems with lateral vibrations from the tool, at distances
greater then 2.5 feet. But, seeing the potential for objections,
we decided to add in a safety factor of 2.0 to the previous
study's findings and require D'arcy & Harty to pothole those
locations."
The 660-foot run was divided into
two sections. The first section was approximately 440 feet long
and ran upstream. A gravity fed system bypass was installed
using 14-inch HDPE. A 6-inch pump was used to assist the bypass
during peak flow times. Three existing 48-inch brick and mortar
manholes along the run were in poor condition and were surcharging
regularly. The manholes were removed before bursting and eventually
replaced with new 60-inch concrete manholes.
The Goliath pipe bursting tool was
fitted with a 34.5-inch OD rear expander. The D'arcy & Harty
crew used a McElroy fusion machine to butt-fuse the necessary
length of 28-inch SDR 17 HDPE. The 20- ton Grundowinch was positioned
upstream, 440 feet away. The crew launched the tool and bursting
was underway. About 5 feet into the run, bursting was halted.
A representative of the San Francisco
Water Department, sent to observe the job, stopped the bursting
almost immediately due to very noticeable surface heaving and
vibrations. Glynn said, "The existing line was very shallow,
with only a few feet deep of cover over the top of the pipe.
We knew there would be surface heaving and vibration, but we
also estimated that lateral vibration would be minimal. From
the studies we looked at, we knew that damaging vibrations,
those above 5 inches per second, would not travel more than
2.5 feet from the bursting head. Now we would have to prove
that."
The SFWD representative requested
that a third party take seismic measurements. Glynn located
a private consultant and had them on site within 45 minutes.
Glynn said, "Four separate
micro-seismographs were set up, on the surface, along the
top of the 79-inch water main, in areas that appeared closest
to the sewer line. While it is hard to know exactly how
far away the micro-seismographs were located from the sewer
line, it is probable that they were as close as 5 to 8 feet.
Results showed that vibrational levels directly over the
water mains did not exceed 0.85 inches per second."
Orton said, "We averaged between
0.42 and 0.48 inches per second which is similar to other large
upsize seismographic job measurements."
The SFWD allowed bursting to continue.
Despite the shallow host pipe, surface
heaving was minimal throughout the first 440-foot run. Additional
seismographic readings were taken during the first burst. Even
though the tool came within 8 feet of the 79-inch water main,
vibrations did not register higher than 0.3 inches per second.
The second burst ran downstream approximately
220 feet. The D'arcy & Harty crew used the same launch pit for
this burst as they did for the first, launching the tool in
the opposite direction. The burst proceeded without problems
until the tool reached a 10-foot PVC point repair approximately
100 feet into the run. The tool jumped out of the pipe and surfaced.
D'arcy said, "We knew about
the repair going into the burst. When we dug up the tool,
we found that an insufficient amount of backfill was used
around the point repair. There wasn't enough friction to
keep the tool on track. It followed the easy path and that
was straight up." Orton said, "There was hardly
any backfill over the existing pipe at that section. There
was maybe a foot of cover at best. If additional backfill
had been placed on the point repair, we wouldn't have had
any trouble. After the D'arcy & Harty crew dug the Grundocrack
up, they lifted everything, re-graded the trench bed, replaced
the pipe and continued bursting without further problems."
Overall, pipe bursting was well received
by all parties involved. Orton said, "We were able to accomplish
a large upsize in an environmentally sensitive area. I think
everyone was pleased."
Glynn said, "While
each job is different and should be evaluated individually,
in the right circumstances, large diameter pipe bursting can
be an effective rehabilitation tool that can dramatically increase
the capacity of an existing system without the disturbance and
cost of traditional excavation and open trench pipe replacement."
Upsizing for the remainder of the
sewer line will go out for bid next spring. Up to 4,000
lf of the 15,000-lf system will include pipe bursting as
the primary replacement method. Jim Schill Technical Writer
Mankato, MN.
Underground Construction,
February 2000, Page R-9
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